Looks like I'm not going to the track in the near future. Since Probe doesn't make this particular piston any more, looks like a full set will be in order. Last time I ran the car was Pinks All Out in Topeka last summer. It was like 110 degrees. I guess the combination of hot, poor machine work, and lean mixture was enough to liquefy part of the piston. At first I thought it was a ring gap issue, but the ring is not damaged, and there are no marks in the head or the piston that would be there had there been a solid chunk of piston dancing around in there. Bummer for me.


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